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Boeing whistleblower John Barnett found dead in US
20 hours
ago
By Theo Leggett,Business correspondent, BBC News
Boeing
A
former Boeing employee known for raising concerns about the firm's production
standards has been found dead in the US.
John Barnett had worked for Boeing for 32 years,
until his retirement in 2017.
In the days before his death, he had been giving
evidence in a whistleblower lawsuit against the company.
Boeing said it was saddened to hear of Mr
Barnett's passing. The Charleston County coroner confirmed his death to the BBC
on Monday.
It said the 62-year-old had died from a
"self-inflicted" wound on 9 March and police were investigating.
Mr Barnett had worked for the US plane giant for
32 years, until his retirement in 2017 on health grounds.
From 2010, he worked as a quality manager at the
North Charleston plant making the 787 Dreamliner, a state-of-the-art airliner
used mainly on long-haul routes.
In 2019, Mr Barnett told the
BBC that under-pressure workers had been deliberately fitting
sub-standard parts to aircraft on the production line.
He also said he had uncovered serious problems
with oxygen systems, which could mean one in four breathing masks would not
work in an emergency.
He said soon after starting work in South Carolina
he had become concerned that the push to get new aircraft built meant the
assembly process was rushed and safety was compromised, something the company
denied.
He later told the BBC that workers had failed to
follow procedures intended to track components through the factory, allowing
defective components to go missing.
He said in some cases, sub-standard parts had even
been removed from scrap bins and fitted to planes that were being built to
prevent delays on the production line.
He also claimed that tests on emergency oxygen
systems due to be fitted to the 787 showed a failure rate of 25%, meaning that
one in four could fail to deploy in a real-life emergency.
John Barnett
John Barnett was a former quality control manager
at Boeing
Mr Barnett said he had alerted managers to his
concerns, but no action had been taken.
Boeing denied his assertions. However, a 2017
review by the US regulator, the Federal Aviation Administration (FAA), did
uphold some of Mr Barnett's concerns.
It established that the location of at least 53
"non-conforming" parts in the factory was unknown, and that they were
considered lost. Boeing was ordered to take remedial action.
On the oxygen cylinders issue, the company said
that in 2017 it had "identified some oxygen bottles received from the
supplier that were not deploying properly". But it denied that any of them
were actually fitted on aircraft.
After retiring, he embarked on a long-running
legal action against the company.
He accused it of denigrating his character and
hampering his career because of the issues he pointed out - charges rejected by
Boeing.
At the time of his death, Mr Barnett had been in
Charleston for legal interviews linked to that case.
Last week, he gave a formal deposition in which he
was questioned by Boeing's lawyers, before being cross-examined by his own
counsel.
He had been due to undergo further questioning on
Saturday. When he did not appear, enquiries were made at his hotel.
He was subsequently found dead in his truck in the
hotel car park.
Speaking to the BBC, his lawyer described his
death as "tragic".
In a statement Boeing said: "We are saddened
by Mr. Barnett's passing, and our thoughts are with his family and
friends."
His death comes at a time when production
standards at both Boeing and its key supplier Spirit Aerosystems are under
intense scrutiny.
This follows an incident in early January when an
unused emergency exit door blew off a brand-new Boeing 737 Max shortly after
take-off from Portland International Airport.
·
US launches Boeing
investigation after blowout
·
Boeing review finds
'disconnect' on safety
A preliminary report from the US National
Transportation Safety Board suggested that four key bolts, designed to hold the
door securely in place, were not fitted.
Last week, the FAA said a six-week audit of the
company had found "multiple instances where the company allegedly failed
to comply with manufacturing quality control requirements".
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