Multiple Failures Put Learjet 35A into the
Atlantic
I thought the days of poorly trained captains and seat-warming copilots
were long gone in turbine operations - at least those conducted in the U.S. But
it would seem there are still operators who are not especially particular about
who's in the cockpit, or their level of competency in the face of unexpected
situations.
This month we'll take a quick look at the loss of a Learjet 35A (XA-USD)
fatal to all four occupants on Nov. 19, 2013, when it crashed into the sea off
the Fort Lauderdale, Florida, coast just 3 min. or so after takeoff.
The NTSB determined the probable cause of the accident was "the pilot's
failure to maintain control of the airplane following an inflight deployment of
the left engine thrust reverser." Further contributing to the accident, it said,
"was the flight crew's failure to perform the appropriate emergency procedures,
the copilot's lack of qualification and capability to act as a required flight
crewmember for the flight, and the inflight deployment of the left engine thrust
reverser for reasons that could not be determined through post-accident
investigation."
The airplane had just completed an air ambulance flight for Air Evac
International from San Jose, Costa Rica, to Fort Lauderdale-Hollywood
International Airport (FLL) and was repositioning back to its base in Cozumel,
Mexico. Weather at FLL included few clouds at 2,500 ft. and a scattered layer at
6,500 ft. The wind was calm and visibility was 9 mi. The temperature was 23C,
the dew point was 22C, and the altimeter setting was 29.93 in. of
mercury.
The Flight
Investigators used FAA ATC voice and radar recordings to determine the
Learjet's track and timeline. The airplane departed Runway 10 at FLL at about
1950 and climbed straight ahead. When it reached an altitude of about 2,200 ft.
and a groundspeed of 200 kt., the copilot requested radar vectors to return to
the runway due to an "engine failure." The controller directed the flight to
maintain 4,000 ft. and turn to a heading of 340 deg. The copilot replied, "Not
possible" and requested a 180-deg. turn back to the airport. The controller
acknowledged, but the airplane continued a gradual turn to the north as it
slowed and descended.
Two minutes later, the copilot declared a "Mayday!" and again requested
vectors back to FLL. During the next 3 min., the copilot requested vectors to
the airport multiple times. While the copilot requested, received and
acknowledged increasingly sharper and tighter turns to the southwest from ATC to
return to the airport, the airplane continued its slow turn and descent to the
north. During the 2 min. following the copilot's declared intention to return to
FLL, the airplane descended to 900 ft. and slowed to 140 kt. as it flew
northbound, parallel to the shoreline and away from FLL.
At 1955:15, the copilot reported the airplane was ". . . 200 ft. over the
sea." After that, there were no intelligible transmissions received from the
airplane, and communications with the airplane were lost.
A search began immediately, but there was no evidence of survivors. Some
floating wreckage was recovered by the U.S. Coast Guard. It showed impact damage
but no evidence of fire. The main wreckage was located on the ocean floor on
Dec. 3, 2014.
The wings were separated from the fuselage, and the outboard section of the
left wing was missing. The left and right wingtip tanks were detached from the
wings. Both ailerons were identified, and one wing flap was found at the
retracted position. Both main landing gear were retracted.
On the throttle quadrant, the left power lever was found past the maximum
position and damage to the forward stop was consistent with over-travel. The
right lever was found one-half inch from its maximum travel. There was no
visible damage to either the idle or cutoff stops.
The thrust reverser control panel and panel chassis were deformed by impact
forces. The internal electronic components were corroded and/or coated with
dried materials indicative of immersion in salt water. The UNLOCK, DEPLOY and
BLEED VALVE annunciator light assembly for both left and right engines appeared
intact. The NORMAL/EMERGENCY STOW switch on the thrust reverser control panel
was found intact in the control panel and in the NORMAL position.
The engine N2 rpm gauges indicated 96.8% on the left engine and 96.5% on
the right. The engine turbine temperature gauges indicated 781C on the left
engine and 780C on the right. The engine fan gauges indicated 89.2% on the left
engine and 89.8% on the right. It would seem the engines had been operating at
near maximum thrust.
Thrust Reverser System
Photographs taken of the submerged wreckage before its recovery from the
ocean floor showed that the left engine's thrust reverser and blocker doors were
not in the stowed position. Examination of components from both thrust reverser
systems (left engine and right engine) after recovery indicated that the
components sustained impact- and seawater-immersion damage. This damage
precluded testing for electrical, pneumatic and mechanical
continuity.
Examination of the left engine's thrust reverser system components found
that the upper blocker door was attached to the reverser and was in a partially
deployed position. The lower blocker door was found hanging from one of its
tension links. The lower blocker door's rod arm was missing a section of its
clamping arm, and the pivoting pins were broken. The lower blocker door showed a
gap between the door skin and door pan with a bend at the forward edge near the
gap. Areas of paint and skin on the left engine nacelle skin and body structure
forward and aft of the cascade exhaust showed discoloration and scorching, with
some paint blistered or missing. The entire perimeter of the outer fan duct
behind which the blocker doors stow (when the thrust reverser was stowed) was
missing.
Examination of the right engine's thrust reverser system components found
that the upper and lower blocker doors were in the stowed position. There was no
visible damage or interference observed between the blocker doors and the
surrounding structure. There was no evidence of heat damage on the engine
nacelle outer skin or paint.
The Pilots
The wreckage examination (and later bench testing) indicated clearly that
the left reverser had deployed in flight. The fact that the airplane ended up in
the water suggested that something went very wrong in the
cockpit.
Both pilots were employed by Vuela SA de CV, which was an independent
company that "leased" the pilots to Aero JL SA de CV. Both companies were owned
and operated by the same individuals.
The pilot held a Mexican commercial pilot certificate with ratings for
airplane single-engine, airplane multiengine land and instrument airplane, and
an ATP and type ratings in Learjets and the Gulfstream GI. The operator told
investigators the pilot had accrued 10,091 total hours of flight experience, of
which 1,400 hr. were in the 30-series Learjet.
On July 5, 2013, the operator issued the pilot a certificate of training
for 8 hr. of crew resource management. On the same day, he was issued another
certificate for an additional 8 hr. of instruction on controlled flight into
terrain.
The copilot held a commercial pilot certificate issued by Mexico, with
ratings for airplane single-engine, airplane multiengine land and instrument
airplane. The copilot's total flight experience could not be reconciled.
Documents provided by the operator suggested the copilot had accrued an
estimated 1,243 total hours of flight experience, of which 29 hr. were in the
Learjet 35.
According to company records and a resume, the copilot began flying
Learjets for the Vuela SA/Aero JL organizations on May 1, 2013. At that time,
the copilot declared 1,206 total hours of flight experience, of which 82 hr.
were "observer" time in Learjet 25s. From the day of employment to the day of
the accident, the copilot accrued 37.16 hr. of flight experience in Lear 25/35
airplanes.
A certificate stamped "General Technical Department of Licenses," which was
forwarded by the operator to the NTSB, suggested the copilot accrued 175 hr. in
the Learjet 35A between July 4, 2013, and Oct. 30, 2013; however, his total
documented flight experience increased only 29 hr. over the same time
period.
On Aug. 20, 2012, the copilot received a diploma for classroom instruction
received for the Learjet 20 series airplanes from a technical training school in
Mexico that had neither airplanes nor flight simulators. There was no evidence
that the copilot completed any training or practical tests in a Learjet airplane
or flight simulator.
On July 5, 2013, the operator issued the copilot a certificate of training
for 8 hours of crew resource management. On the same day, he was issued another
certificate for an additional 8 hours of instruction on controlled flight into
terrain.
Pay records for the pilot and copilot show identical hours, deductions, and
pay over several consecutive pay periods. The pilot and copilot had flown
together on three occasions before the accident flight. The accident flight was
their first flight together in the United States.
The Safety Board said a search of student records by "two prominent Learjet
training vendors in the United States" revealed no records of simulator flight
training or attendance by either the pilot or copilot. Emergency procedure
training for an inflight deployment of a thrust reverser could be performed only
in an appropriately equipped flight simulator.
The Director General of Civil Aeronautics (DGAC) for the government of
Mexico examined the pilot and flight training records for both pilots and
summarized their findings for the NTSB report:
"Both the pilot and copilot records showed inconsistencies on the
verifications of training and certifications based on the way official
government stamps and certifications were displayed over, and with, the entries.
They were copies, and did not represent entries properly certified by the
Government of Mexico."
Some of the captain's experience and certifications were based on logbooks
never presented. The copilot's records showed the training for the Learjet 20/30
series airplanes provided and conducted exclusively by the operator, Aero JL.
Further, there was no "original foreign license and logbook," no "official
license certificate" or DGAC file records to support a claim that the copilot
had 1,243 total hours of flight experience.
According to the DGAC, the copilot had actually accrued only 206 total
hours of flight experience. The copilot was evaluated by the DGAC in the
airplane on May 2, 2013, and his performance during the practical test was found
to be "unsatisfactory."
The CVR
The transcript of the cockpit voice recorder (CVR) certainly reflected the
training situation just outlined.
No checklists were called for, offered or used by either crewmember during
normal operations (before or during engine start, taxi, takeoff) or following
the announced inflight emergency. There were no challenge-and-response checklist
callouts between the pilot and copilot at any time during the flight, no
elements of crew coordination and no identification of the
emergency.
After the "engine failure" was declared to ATC, neither crewmember asked
for or offered the "Engine Failure" checklist, nor was there any attempt to
complete an emergency procedure and then ask for a checklist verification of
actions taken. The pilot asked the copilot for unspecified "help" because he did
not "know what's going on" and he could not identify the emergency or direct the
copilot in any way with regard to managing or responding to the emergency. At no
time did the copilot identify or verify a specific emergency or malfunction, and
he did not provide any guidance or assistance to the pilot.
According to Learjet, in the event of an inflight emergency, the typical
convention was for the pilot flying to fly the airplane and take over
communications with ATC. The pilot monitoring should then complete the
appropriate checklist, while audibly announcing his actions as they are
completed. The pilot flying was to verify these actions prior to completion.
Although different flight departments may adopt their own procedures, there was
no evidence that any crew coordination actions took place on the accident
flight.
Specifically, the Safety Board said, "Based on the wreckage evidence and
data recovered from the left engine's digital electronic engine control [DEEC],
the thrust reverser rocker switch was not placed in the "EMER STOW" position,
and the left engine was not shut down.
"The DEEC data showed a reduction in N1 about 100 sec. after takeoff
followed by a rise in N1 about 35 sec. later. The data were consistent with the
thrust reverser deploying in flight [resulting in the reduction in N1] followed
by the inflight separation of the lower blocker door [resulting in the rise in
N1 as some direct exhaust flow was restored].
"Further, the DEEC data revealed full engine power application throughout
the flight. Although neither flight crewmember recognized that the problem was
an inflight deployment of the left thrust reverser, certification flight test
data indicated that the airplane would have been controllable as it was
configured on the accident flight. If the crew had applied the "engine failure"
emergency procedure [the perceived problem that the copilot reported to the air
traffic controller], the airplane would have been more easily controlled and
could have been successfully landed."
Unwanted TR Deployment
Manufactured in 1979, the accident airplane was powered by two Garrett
(Honeywell) TFE731-2 turbofan engines. Its most recent continuous airworthiness
inspection was completed Nov. 4, 2013, at 6,842 aircraft hours.
The Lear was equipped with an Aeronca Inc. 45-1000 thrust reverser system.
When reverse thrust was commanded from the cockpit during a landing roll, the
thrust reversers operated to reverse the direction of the engine exhaust gases
to assist with stopping the airplane on the runway. The thrust reversers were
designed to deploy only when the squat switches were in the "weight on wheels"
mode and the throttles were in the idle position. When activated, the thrust
reverser system used 28-volt power for reverser control and engine bleed air to
deploy the translating structure. The electrical system in the thrust reverser
incorporated an automatically initiated "stow" command if the pneumatic latches
became unlocked in flight.
A rocker switch in the cockpit could be positioned to either "NORM"
(normal) or "EMER STOW" (emergency). Three indicator lights in the cockpit for
each thrust reverser provided the flight crew with thrust reverser status and
position information. These lights, "UNLOCK," "DEPLOY" and "BLEED VALVE,"
illuminated and extinguished during the application and stowing of the thrust
reversers. The "UNLOCK" light would remain illuminated any time that a thrust
reverser pneumatic latch disengaged or was not in the locked configuration after
a thrust reverser was stowed, or if a thrust reverser failed to stow
completely.
The AFM Aeronca TR Supplement stated "an inadvertent thrust reverser
deployment during takeoff will be indicated by illumination of the affected
thrust reverser UNLOCK and/or DEPLOY lights." If this occurred below V1 speed,
an aborted takeoff should be performed. If this occurred above V1 speed, the
flight crew should maintain directional control, reduce the affected engine
thrust lever to idle, place the NORM-EMER STOW switch to EMER STOW and continue
the takeoff.
The procedures stated that, "If UNLOCK or DEPLOY lights do not go out,
Thrust Lever [affected engine] - CUTOFF." The procedures stated that the ENGINE
SHUTDOWN IN FLIGHT procedure in the basic AFM should be performed.
The AFM Supplement also contained "Abnormal Procedures" for an inadvertent
thrust reverser deployment in flight. Those procedures also specify that, if the
UNLOCK or DEPLOY lights do not go out, the ENGINE SHUTDOWN IN FLIGHT procedure
should be performed, followed by the SINGLE-ENGINE LANDING procedure from the
basic AFM.
Safety Board investigators reviewed airplane manufacturer's records and the
NTSB accident and incident database and found no previously documented instance
of an un-commanded inflight deployment of a thrust reverser on a Learjet
35.
Bottom Line The airplane required two fully qualified flight crewmembers;
however, the copilot was not qualified to act as second-in-command on the
airplane, and he provided no meaningful assistance to the pilot in handling the
emergency.
Further, although the captain's records indicated considerable experience
in similar model airplanes, his performance during the flight was highly
deficient. Based on the CVR transcript, the pilot did not adhere to industry
best practices involving the execution of checklists during normal operations,
was unprepared to identify and handle the emergency, did not refer to the
appropriate procedures checklists to properly configure and control the airplane
once a problem was detected, and did not direct the copilot to the appropriate
checklists.
In short, this was a totally unprofessional operation masked as something
well run with well-qualified personnel. And four people and an aircraft were
lost as a result of that dangerous illusion.
This article appears in the May 2016 issue of Business & Commercial
Aviation with the title "Total Failure."
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