Inquiry alleges tampering
of hard-landing A321 cockpit recorder
By David Kaminski-Morrow25 May 2020
Russian investigators probing an Airbus A321 hard landing have made the
extraordinary accusation that its cockpit-voice recorder was erased and fitted
in another aircraft, then re-installed in the damaged jet, ahead of the inquiry
commission’s arrival.
The Nordwind A321 – on final approach to Antalya’s runway 36C on 10
January – sustained serious damage after the aircraft, which had slowed below
its lowest selectable speed threshold moments before touchdown, was abruptly
pitched down and struck the runway nose-gear first.
Its crew subsequently executed a go-around, with multiple system
problems emerging, before landing on the same runway. None of the seven crew
members, the only occupants, was injured.
Source:
Interstate Aviation Committee
Flight-data information showed the A321 hit the runway nose-gear first
But in its preliminary factual findings from the accident the
Interstate Aviation Committee says that the cockpit-voice recorder, while being
analysed in Moscow, revealed only a few seconds of information.
It says this indicates the button to erase the cockpit-voice recorder
“was pressed in the cockpit”.
Investigators used specialist techniques to retrieve just over 2h 4min
of recordings, but found there was “no record” of the incident on 10 January.
But there was a record of a subsequent flight – the next day, 11
January – by a different Nordwind A321 flying the route from Antalya to Moscow
Sheremetyevo.
There were also recordings of Russian maintenance personnel at
Sheremetyevo carrying out maintenance on 11-12 January, and then discussions on
13 January including remarks about pushing the cockpit-voice recorder ‘erase’
button.
The Interstate Aviation Committee says it was informed of the accident
on 14 January.
Although investigators found the cockpit-voice and flight-data
recorders fitted on the damaged aircraft, the operator already had a copy of
the flight-data recording. Both recorders were sent to Moscow for analysis,
where the missing cockpit-voice information was discovered.
The inquiry believes that, in the aftermath of the accident to the A321
(VQ-BRS), both recorders were removed and taken to Antalya’s RMS Technic
maintenance facility, and the voice recorder was fitted to a second A321
(VP-BHN) flying the return service to Moscow.
After this A321 arrived in Moscow, it was removed by another maintenance
firm, NW Technic, and – in hand luggage on an Aeroflot flight – transported
back to RMS Technic in Antalya where the recorder was refitted to the original
damaged A321, before the inquiry team arrived.
“The [inquiry] believes the loss of information recorded [on the
cockpit recorder] of VQ-BRS became possible as a result of non-compliance by
officials of [the airline and maintenance companies],” it says, pointing out
that pre-emptive retrieval of flight-recorder information is prohibited.
FlightGlobal has contacted Nordwind, NW Technic and RMS Technic for
comment on the investigators’ findings.
The inquiry has recommended that Russian and Turkish regulators
“evaluate the actions” of officials of the three companies regarding the loss
of the cockpit-voice recording.
Source:
Interstate Aviation Committee
Substantial structural and aircraft systems damage resulted from the
impact
Analysis of the accident sequence determined that the autopilot and
autothrust were disengaged during the base leg and the aircraft was flown
manually during the final approach.
The crew lowered the landing-gear at 164kt, while at 1,500ft and 5.4nm
from the runway, and selected full flap. At 3nm and 1,035ft the aircraft was
stable.
But as it descended below 270ft – about 100ft above ground – its
airspeed began to fall below the approach speed of 122kt. It further decayed to
115kt, below the lowest-selectable speed threshold of 117kt, while descending
at 700ft/min.
At 20ft above the runway the airspeed reached its minimum of 109kt,
with the aircraft pitched 5.5° nose-up, idle thrust was selected.
Then the captain abruptly moved the sidestick fully forward, holding it
there for 1.5s, resulting in a sudden, sharp reduction in pitch at a rate of
9°/s.
Although the captain simultaneously applied full thrust, the aircraft
had pitched nose-down by 3.9° and its nose-gear struck the runway with a 2.64g
impact. It bounced and the captain pulled the sidestick, while sidestick input
also registered from the first officer’s position.
Several systems immediately began to fail. The A321’s flight-control
system switched to direct law, two inertial reference systems failed, and
attitude indications disappeared from the captain’s instruments. Although the
flaps were partially retracted during the go-around, the landing-gear could not
be retracted – the crew claimed the lever jammed.
The first officer was given control of the aircraft, because the
attitude indicators were still functioning on the right side, and trimmed it.
As the aircraft reached 920ft an avionics smoke alarm triggered and the
crew declared an emergency. The third inertial reference system failed at
3,400ft, the attitude indicator on the first officer’s side disappeared, and
the captain retook control.
The crew carried out a flypast for a visual inspection of the
landing-gear before attempting another approach. As it passed over the runway
the crew received alerts about two different hydraulic circuits. The inquiry
says a total of 103 failure messages, concerning various systems, were
received.
With the landing-gear confirmed in the deployed position, the crew
completed the approach and landed on runway 36C where the A321 came to a halt.
In its analysis the Interstate Aviation Committee, which published its
findings in April, made a number of recommendations about improved awareness of
stable approach criteria, go-around procedures, and prevention of hard
landings.
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