Cleared-to-land Ryanair
737 crew warned tower about occupied Porto runway
By David Kaminski-Morrow14 July 2023
Portuguese investigators have disclosed that a Ryanair Boeing 737-800
crew on approach to Porto warned air traffic control that the runway was still
occupied despite having received landing clearance.
The incident on 26 June occurred after an Azores Airlines Airbus
A321neo was authorised to line up, behind landing traffic on short final, on
runway 35.
Portuguese investigation authority GPIAAF says the approaching traffic
landed and the A321neo (CS-TSI) lined up to await take-off instructions.
The Ryanair aircraft (EI-DLX) had also been on final approach to the
runway.
According to GPIAAF its crew contacted air traffic control, about 30s
before touchdown, receiving landing clearance and wind information.
“The [Ryanair crew], noticing that the runway was occupied by the
Airbus, warned the controller of this fact,” states the authority.
The controller cancelled the landing clearance and ordered the 737 to
execute a go-around about 13s ahead of its reaching the runway 35 threshold.
Source: FlightGlobal from
GPIAAF/Google Maps data
Controllers had cleared the Ryanair flight to land while runway 35 was
occupied by the A321neo
GPIAAF says a preliminary analysis indicated the 737 was 275ft above
ground and 950m from the runway, where the A321neo was positioned.
The A321neo departed for Porto Santo and the 737 subsequently landed,
without further incident, after a second approach. No-one on board either
aircraft was injured.
Meteorological data from the airport shows good daylight weather
conditions at the time.
GPIAAF says the Porto tower controller has responsibility for the
ground control function, which is normally performed by a dedicated controller.
It adds that several departing aircraft had been in contact with the tower at
the time of the event.
The authority had recently completed an inquiry into a similar
occurrence at Porto, in April 2021, during which an ASL Airlines Belgium
737-400 had been cleared to take off from runway 35 despite the presence of an
inspection vehicle.
Investigators determined that the controller had carried out a 4h solo,
uninterrupted shift before the incident.
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