fredag 11. mai 2018

Motorproblemer - Curt Lewis


Incident: American B738 at New York on May 10th 2018, engine failure
An American Airlines Boeing 737-800, registration N843NN performing flight AA-2229 from New York La Guardia,NY to Orlando,FL (USA) with 156 passengers and 6 crew, was climbing out of New York when the crew requested to maintain 12,000 feet while they were troubleshooting a problem. The crew subsequently advised they had an engine failure and wanted to divert to New York's JFK Airport. The aircraft landed safely on JFK's runway 22R about 20 minutes later.

The airline reported the engine had no visible damage, the crew had received an engine fault indication which subsequently was identified to have been caused by the engine oil filter.

A replacement Boeing 737-800 registration N894NN reached Orlando with a delay of about 2 hours.
  
 

 

Incident: Jazz DH8D at Timmins on Apr 30th 2018, engine shut down in flight
A Jazz de Havilland Dash 8-400, registration C-GJZR performing flight QK-8284 from Timmins,ON to Toronto,ON (Canada) with 54 people on board, was in the initial climb out of Timmins when the left hand propeller's RPM dropped to 850, then accelerated to 1060 (overspeed condition). The crew worked the related checklists, shut the left hand engine (PW150A) down and returned to Timmins for a safe landing.

The Canadian TSB reported maintenance replaced the propeller PCU.

 

 

Incident: Lufthansa Cargo MD11 at Frankfurt on May 8th 2018, rejected takeoff due to engine failure
 
A Lufthansa Cargo McDonnell Douglas MD-11, registration D-ALCE performing freight flight GEC-8340 from Frankfurt/Main (Germany) to Tel Aviv (Israel), was accelerating for takeoff from Frankfurt's runway 18 when the crew rejected takeoff at high speed (about 110 knots over ground) due to the failure of the #3 engine (CF6, right hand). The aircraft slowed safely and stopped about 1000 meters (3300 feet) short of the runway end. Emergency services responded and checked brakes and engine.

The aircraft was towed to the apron, the runway re-opened about 50 minutes after the rejected takeoff.

A ground observer reported the #3 engine emitted a loud bang and a streak of flame followed by less loud bangs and streaks of flames in regular intervals. The aircraft slowed and stopped on the runway.

The right hand engine just "coughing":


 

 

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