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Accident: Transnorthern DC3S at Anchorage
on Dec 8th 2021, engine failure and gear up landing
A Transnorthern Aviation Douglas DC-3 (C-117 Skytrain), registration N28TN
performing freight flight TNV-123 from Anchorage,AK to Kodiak,AK (USA) with 2
crew, was in the initial climb out of Anchorage's runway 07L when the crew
declared emergency due to the failure of the right hand engine (R-1820),
initially requested to return to runway 07L requesting left turns only but in
the turn decided to divert to Anchorage's Merill Field, located 4nm to the
northeast of Anchorage's International Airport. After reaching a maximum
altitude of about 900 feet the aircraft performed a gear up landing on Merill's
runway 07 keeping the left wing up (and engine operating) as long as possible.
The crew was able to bring the aircraft to a stop on the runway. There were no
injuries, the aircraft sustained substantial damage.
The NTSB reported the aircraft experienced a loss of engine power shortly
after takeoff and made an emergency landing at Merill with two pilots on board,
the aircraft was still gear up when the aircraft touched down on runway 07 at
Merril. There were no injuries. An investigation has been opened.
The aircraft was recovered from the runway by a crane, the runway was
returned to service about 6:15 hours after landing.
Accident: Transnorthern DC3S at Anchorage on Dec 8th 2021, engine failure
and gear up landing
A Transnorthern Aviation Douglas DC-3 (C-117 Skytrain), registration N28TN
performing freight flight TNV-123 from Anchorage,AK to Kodiak,AK (USA) with 2
crew, was in the initial climb out of Anchorage's runway 07L when the crew
declared emergency due to the failure of the right hand engine (R-1820),
initially requested to return to runway 07L requesting left turns only but in
the turn decided to divert to Anchorage's Merill Field, located 4nm to the
northeast of Anchorage's International Airport. After reaching a maximum
altitude of about 900 feet the aircraft performed a gear up landing on Merill's
runway 07 keeping the left wing up (and engine operating) as long as possible.
The crew was able to bring the aircraft to a stop on the runway. There were no
injuries, the aircraft sustained substantial damage.
The NTSB reported the aircraft experienced a loss of engine power shortly
after takeoff and made an emergency landing at Merill with two pilots on board,
the aircraft was still gear up when the aircraft touched down on runway 07 at
Merril. There were no injuries. An investigation has been opened.
The aircraft was recovered from the runway by a crane, the runway was
returned to service about 6:15 hours after landing.
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